Top Flite 60-90 size P47 ARF… Gas to Electric P3: Motors, Speed Controllers and Batteries

This is part 3 on my journey of converting this aircraft to Electric power.  To see the previous post on the topic, click here.  

As I have mentioned previously, I had picked up a nice Hacker motor from a flying club member and it seemed like it might work out as a power plant for this aircraft.  I needed to get that mounted and also figure out what sort of ESC might be appropriate as well as selecting an appropriate battery and then figure out placement and mounting for all of that.  So here was my process.

First I researched the airplane, including expected weight, wing area and ground clearance.  I also read a bit on any balance issues folks reported to see if I was likely to need nose weight or tail weight and the weight of the suggested power plants.  Armed with that I logged into ECalc and filled in the blanks with the wing area, weight and the motor type I had on hand.  I then started plugging in appropriate speed controllers, props and battery combinations to see what I was going to need to get a good power to weight ratio.  Something in the 1.2:1 or higher range seemed like a good goal for a fighter aircraft like the P47!

I like to keep the voltage high and amperage low in an RC aircraft power system.  Higher amperage is hard to accommodate as most of our common connectors are not rated for it.  If you overtax them, they get hot and waste power and eventually this causes a catastrophic failure.  For similar reasons, our LiPo batteries will fail quicker when you run demand high current rates from them, plus they cost and weigh more as you try to accomplish this with batteries that have a higher “C” rating. 

A little rant about LiPo C ratings…   Feel free to skip the next two paragraphs if you like.

In general, C ratings are useful only in that a higher C rating within a manufacturer battery line indicates the ability to supply more current without damage to the battery than the batteries with lower C ratings.  Beyond that they are deceptive at best and almost useless for comparison between manufacturers.  Feel free to disagree but I am convinced that this is the state of things at this time and don’t expect it to change anytime soon so don’t put to much faith in C ratings.

So, while my large aircraft could (according to the manufacturer C rating) run on 20C cells, typically 40C cells get pretty hot and therefore fail sooner rather than later.  The 50-60C packs simply perform better, don’t get as hot and outlast the lower C ratings… at least in the brands I most commonly run.  I don’t bother to purchase from companies who advertise 100C and better as they are pure fiction in my opinion.  A continuous draw at the advertised C rating is almost always a recipe for battery destruction in very short order and in the case of larger capacity packs is likely going to result in batteries dying from internally generated heat and wires/connectors or something similar failing anyway as the system quite literally “melts down”!  It’s a joke to say you have a 4000mah 100C pack (that equates to 400A draw) and then putting a connector on it that is rated to handle, maybe 100A for short periods before it literally “melts down”!   The cells in these packs might handle 150A draw with perfect ventilation but I doubt it.  OK, rant over.

Back to sizing the system I came to the conclusion that running an 8S system with a 16×10 prop would be a good starting point with a predicted 1.3:1 thrust ratio.  Partly this choice was based on the power I wanted and partly due to available speed controllers.  Spektrum had just released a line of Avian speed controllers and one of them was capable of 8S (which I estimated was close to the biggest packs I could likely get into the airplane) and was rated at 80A continuous with 100A peaks which was as much as I really wanted to run through the EC5 connectors anyway!  It was also far less expensive than the Castle Creations options in this same range and had Telemetry built in that I was going to want.  I can do that with Castle Creations and most other speed controllers as well, but with even more expense.  This setup also allowed me to prop up a bit for additional power if I later decided I needed to, which is always a nice option to have.  The tradeoff if I did was that a 16×10 would likely give me 7 minutes or more in the air with a 5000mah pack while a 17×10 or 18×10 would start to cut into that as they would draw more amps.

In order to take advantage of the telemetry capabilities I wanted to access from the Avian speed controller I also would have to acquire a new receiver.  I settled on a new AR6610T.  That wouldn’t be a terrible expense as I had a project that needed a simple receiver like what was currently installed in the P47 so one way or another I was going to be buying one soon anyway.

Decisions made, I placed some orders and started looking to mount the motor.   This came down to simply finding the right size spacers and then a hole for the wires to get through the firewall and some judicious trimming of the dummy engine.  

The spacer length I needed turned out to be the same as some readily available standoffs for a DLE 30, which simplified things a bit.  

Then to allow the prop to clear the cowl I added a couple washers behind the prop collet assembly.

Accommodating an already existing 6S 5000mah pack plus a 2 cell pack of equal size and rating in series (which the speed controller accommodates simply as it already has a series harness attached!) was a bit tricky as the tray exposed under that hatch was simply too shallow for this setup and I didn’t want to buy several batteries for which I would have no other use.  Here’s the original space.

So, I did some cutting and regluing to create a “ramp” that allowed for easy insertion of some of the packs I had.  I had already determined that having the batteries up against the back of the firewall was appropriate to get the balance where I wanted it and while it was a bit tricky to cut out, the existing structure, thusly relocated, works well for the new battery compartment “floor”.

I needed some 2S “booster” packs (as I think of them) to add to my 6S packs in order to run an 8S system so I started looking for something appropriate.  I ended up with some APower branded 5000mah, 60C rated packs I picked up from RCBatteriesusa based in Arizona.  I had read an article about the company recently and decided to give them a try.  They are not the cheapest place to buy packs, but not at the very high end either and offer a good warranty as well as being reputed to have top notch service.  The folks there were as good as advertised in taking care of what I wanted, including the fitting of my requested EC-5 connector even though that was not an option on the web site when I first started shopping.  At no additional cost I might add.  After unpacking, examination and a few cycles they appear to be high quality.

That about covers the power system… I think.  Next time I’ll try to run down my experiences and impressions of the first dozen or so flights.

Top Flite 60-90 size P47 ARF… Gas to Electric P2: The Hidden Battery Hatch

For Part 1 of this article, click here.

It was the wee hours of the morning before I really made the firm commitment in my mind that the P47 had to make the conversion to Electric.  At the next opportunity I started the process.

First order of business was to pull all the gas accoutrements from the airplane.  First, I pulled the prop and cowl and started stripping out the gas motor mount, ignition and the supporting switch, battery etc…  I knew a guy who was looking for a  DLE-20 so I made him a deal on the engine to help finance the needed items to complete the conversion.  I had the motor but needed a speed controller and maybe some additional lipo packs.

As soon as all that was out of the way it was time to explore the “hidden hatch”.  For reasons that are beyond my comprehension, Top Flite built a hatch into the top of the P47 (and other models in this line of ARF warbirds).  They framed it out in ply, put magnets in place along with pins to hold it in place… and then put a solid balsa sheet skin over the entire nose (including the hatch) and covered it with no markings or indication that it existed.  Nor is it documented in any way in the manual!

With no guidance it became quite the task to figure out how to outline and cut the hatch free.  What I eventually settled on was to take a pair of forceps with an extremely sharp needle locked in it’s jaws and reach down into the wing saddle and force it up between the two plywood plates at each end and side of the hatch until it emerged through the covering.  By doing this repeatedly, working my way around the hatch perimeter I outlined the hatch on the covering.  Then while holding my breath, holding my head at just the right angle and sending up prayers to the modeling gods (a more fickle lot I have yet to meet) I took an Xacto knife and inserted it into one of the pin holes and slid it by feel between the plywood plates.  Working my way around the perimeter of the hatch, I managed to slice my way through the vast majority of the sheeting.  With the judicious use of my razor saw, I got the hatch loose with only one problem… I managed to cut through the pins at the aft most part of the hatch! 

Don’t worry about the wasp decal… I was planning on ordering replacement graphics anyway!

As you can see it wasn’t a perfect cut but it came out well enough!

   

Luckily, I had on hand an appropriate sized dowel and replacement of the pins proved to be a fairly minor task.  I would later go on to add a hatch latch on the leading edge of the hatch… or at least on the new one I had to build after I found out the hard way that those magnets just aren’t strong enough!

Next time I’ll discuss the power system choices I made and how that is working out.

To see the next post on this topic click here.

 

Top Flite 60-90 size P47 ARF… Gas to Electric P1: Decisions

I already posted a bit here about this airplane with the focus on the retracts I used.  You can see that post here.  This post will focus more on the Electric conversion process and the results of that.  Note that I never flew the plane with the DLE 20 that was on it when I acquired it so can’t compare to that… I can only tell you about my conversion process and the results I got.

Acquiring the airplane

I have a flying buddy that has been in and out of the hobby for the past several years named Martin.  Martin called me after not having heard from him for a bit (maybe a year or more) and reminded me of a P47 that we had worked together to get ready to fly.  It was a 60-90 size Top Flite ARF and we had gotten it pretty close to flyable with a DLE 20 installed, servos and linkage all installed and even radio gear all in place.  For whatever reason it had just never made it into the sky.

Martin asked if I was interested in the airplane.  If you look back at my previous posts you will see that I already own a nice FMS 1500mm P47 that flies very well on 6S.  While I have a particular affinity for the P47 (my grandfather helped build them in Evansville, Indiana during the war) I was hesitant because this airplane is only slightly larger than the foamy I have and I wasn’t sure I really needed two P47s in a very similar size… plus I’d have to consider whether to convert it which might be quite a job.  Add in that I really didn’t have any room in the RC budget at that moment for another airplane and I explained to Martin that I really couldn’t give him nearly what it was worth.  Martin however, explained that he simply wanted to get out of the larger airplanes like this and since I had spent so much time working with him on it, he was simply offering to give it to me!  I offered to at least pay something but Martin insisted that if I had an interest that it was mine.  He even offered to deliver to the field in a couple days when I was planning to fly.  What could I say?  Of course I accepted.

Here’s what she looked like just after delivery.

 

Modifications and Decisions

After a lite cleaning and a thorough inspection I made a couple decisions on things I wanted to change/upgrade or just tinker with a bit before I’d fly it.  A couple were easy decisions. 

First, I wanted to order a new set of graphics as the decals the came with the plane I knew would never last.  In my experience if you want good looking and long lasting graphics with few/no wrinkles or bubbles you buy vinyl… typically from Callie Graphics.  Callie is inexpensive, willing to work with you on any request and provides a great product.  I had a set of markings on a 50cc size Mustang for 3 or 4 seasons.  Many days the plane sat out in the sun all day and the vinyl never bubbled or faded.  I even had to peel the stars and bars from the wing and reapply them when I crashed the bird and bought a new wing.  They still looked like new when I sold the plane a few years ago.

Second, I knew I wanted to replace the landing gear, which I’ve already discussed.

The third issue was much more of a question and it took a couple weeks to come to a conclusion.  What to use for power?  Obviously leaving the DLE 20 in place would have been easy.  I knew the history of the engine and that it ran well before it came to be installed in this bird and it would certainly be an adequate power plant.  However, every other plane I currently own is electric and I had what I thought might be an excellent motor for the purpose.  In fact I had been looking for something to put the motor in ever since I acquired it.

Thus began several days of reading and research.  First I looked on various discussion groups about the airplane and what others had done.  90% plus had run gas engines… a few 2 stroke glow and a few 4 strokes rounded out the vast majority.  What intrigued was the 2 guys who mentioned they were running electrics.  Eureka!  Until I realized that there was just no easy place to put a battery hatch into the P47… at least not that I wanted to tackle.  the plane is pretty much all curves and being an ARF, access is limited unless you want to recover and rebuild extensively.  This didn’t seem promising.

While I mulled on that, I started to look into the electric motor I had and tried to figure out if it would be enough power for the P47.  The motor is a Hacker A60-5S-V2 and while the Hacker site has a fair amount of info there was only a bit of corroborating information that I could find.   It looked like it might be just a bit on the small side if you believed the Hacker site information.  Encouragingly, the actual users reported fairly uniformly that they were running this motor (and most Hackers it seemed) at the maximum ratings and even significantly above with no problem at all.  I picked up this motor at a swap meet NIB from a trusted source at about half the price of a new one… I could never bring myself to pay the full price when there were a lot of quality motors available at much lower prices… Could the Hackers really be that much better??  This was my chance to find out, right? 

With 90% of my previous electric setups I was always able to find a dozen examples of similar planes and power plants to compare to.  In this case, only a couple examples were out there… so lacking enough information to confidently pick a proper propeller and speed controller I decided to revisit an old standby… eCalc.  I won’t go into great details, but based on what it showed me I decided that the Hacker could “hack it” on the P47.   I might need to use 8S batteries (which I have none of) and the flights might be a bit shorter than I’d ideally like (6-7 minutes predicted) but I really wanted to try out this motor. 

So that issue aside I was back to the problem of a battery hatch…  I went back to all the groups and started reading again and after several hours of reading and making the firm decision to just keep the DLE-20 in place, I read a few more posts and one of the guys who was running electric power mentioned the hidden hatch… WHAT!?  I read on for hours and found nothing but then I saw reference that the hatch existed on this entire series of warbirds??  It was only 1AM by this point and I had to get up at least by 6 but this was important, right?  As I continued my research, I found a description of where the hatch was located and how to open it up on the sister warbird, the Mustang.  A quick trip to the shop and I confirmed the hatch did actually exist on my P47 as well… sort of… and the decision was made.  I had to try.

To see the next post on this subject click here.

 

 

E-flite 60-120 size retracts

I recently came into possession of a Top Flite 60-90 size P47 ARF.  It had a DLE 20 on it and was nearly in a ready to fly state and had never been in the air, but of course I couldn’t just leave it alone.  I have zero non-electric aircraft in my fleet at the moment and it so happened I had the perfect electric motor sitting in the box… so of course I converted it immediately!  I also knew that one of my flying buddies was in the market for the exact gas engine that was installed in the plane.  Thus it began.

I won’t go into detail here about the whole conversion.  For more details on that there are several posts starting with this one: P47 Conversion.  Suffice it to say that just when I thought it was fully ready to fly, now under electric power, I ran into a problem with the landing gear. 

The landing gear that came with the plane was a mechanical retract system with “plastic” mechanisms and it had a lot of slop in the system.  Even when fully locked up or down the gear could rotate… perhaps 3-5 degrees.  The result was the wheels would not stay tucked up in the wheel wells, nor did they maintain the proper angle when down and “locked”.  I first realized how big a problem this was likely to be when I taxied the plane around in my driveway.  After rolling 5-10 feet it was like applying the brakes.  You could see the wheels tilt inward at the pavement and twist inward so that they started scrubbing against the concrete.  It was obvious this was not going to work.  If I got off the ground at all, surely any landing with the wheels deployed was going to result in a flip over.  With an 11lb plane, a flip over was likely to result in some consequential damage.

Then the question became, what to do?  I disassembled the existing retracts and looked at any possibility for improving/repairing what was there but I could not come up with an adequate plan.  I could also go to one of two “big names” and get retracts for the airplane… whether they be mechanical, electric or air driven.  I was concerned the mechanical systems from the big names might put me right back where I was (at worst) or work OK, but cost me $150 at best… and of course their electric sets, which I have used before are very pricey.  I could easily have spent $300 or more on those.  I had not intended to spend much money to get this airplane flying but there was no fixed gear option so I had to do something.  I really wanted to go electric but the cost…

Fortunately I read on some forums how guys had put some E-Flite electric retracts in the plane and claimed they worked well.  I take anything I read on the forums with a grain of salt.  I’m convinced most will not admit that they are unhappy with something they spent a lot of money on and are now stuck with so I wasn’t sure.  I tried to read the specs/look at dimensions etc… but unfortunately this is a brand from Horizon Hobby and their web site is simply pathetic.  Not only is their search engine on the site total crap, but they typically provide very limited information on their products on the site and these were no exception.  No indication of the build material, no dimensions, no complete description or listing of what parts come in the box, etc…but having few other options coupled with some good reviews in the discussion threads I was reading combined with an affordable price convinced me to take the plunge.

Immediately on picking them up from my local hobby store I was cautiously impressed.  These thing looked like they were machined from aluminum and what’s in the box is very complete, down to the necessary allen wrenches provide (3) to fit all the set screws!

Here’s the box contents…

And here is a closer shot or two of the mechanism itself.  

To me, these are things of beauty, and I only paid about $155 for the pair through my local hobby shop, including tax!

It took a little work to get them into the bird… nothing terrible and none of it reflecting badly on the retracts.  Since installing these I have made I think 10 flights.  I fly off of grass and Geotex runway and there has been no rain in the last 10 days before my last flights yesterday so the ground is hard and there are some bumps out there as well and so far these things have worked flawlessly.  Not one time have I had an issue with either retract failing to move when commanded, coming up short of full motion, twisting wheels, nose overs… etc…  From a functionality perspective, I have nothing but high praise for the E-Flite retracts.

If your looking at these and trying to decide if they are worth the money, I’d say yes.  Further if you are trying to figure out how well built they are, I would say they are top notch.  I’ve seen nothing to indicate that this is anything but top quality throughout.  Finally, of course the information you need to see if these will fit is not to be found.  So here are some measurements for you in case you need them.

I’m using English/US measurements and I’m sure these were made using metric measurements so these are approximate.

Across the mounting tabs the retracts are 1.75″ wide and 1.5″ long.  Each tab is 15/32″ (just under a half inch) across the outer face.  The depth of the units measured from the back of the mounting to the bottom is 1 and a 16th and the part that extends down into the wing is about 13/16ths wide.  The mounting tab itself is approximately 3/16ths thick.  The units themselves are approximately 3.25″ long (measuring the metal “frame”) which includes the motor mount etc…  The strut is 5mm in diameter which allowed me to use my existing strut with just a minor trim at the top so that the “curly q” shock absorber bend in the struts lined up with the cutout in the wing.

Hopefully some of that will be useful to others out there.  Wouldn’t a dimensional drawing from E-Flite be nice!!  Still the units are top quality and reasonably priced!  If your in the market, I don’t think you’ll be unhappy with these.

Parallel Charging… don’t do what I did!

For those of you who are at least somewhat seasonal flyers like I am, you may recognize the dangers of the first few trips to the RC field after being mostly away from flying for some weeks or months.  There are new planes to fly, old problems with existing planes that you promised yourself you’d fix over the winter and of course just the early season issues caused by being out of the groove.

I recently had one of those “early season” moments (at least that’s what I’m going to blame it on) where I did something stupid because I didn’t have my head in the game when it mattered.  Here’s what I believe occurred.

My first mistake was in not being prepared.  Usually, when I get to the field I have already charged up flight packs and my radio, insured I have all the right bolts, tubes and whatever for the planes I intend to fly, etc… but this time I just didn’t get the proper time to prep so I arrived at the field with the two batteries I had for the plane I most wanted to fly in storage mode.  So I pulled out the generator, hooked up my power supplies, grabbed the high power charger and popped the two 5S batteries on the parallel board to charge.  Of course I did this all in a hurry and without putting my glasses on.

That’s when the fun began.  As I was starting to program my charger, the smell of burning plastic and some smoke started to issue from the area of the batteries!  I quickly yanked the battery connections lose and tossed the batteries into an open grassy area away from any nearby cars and my trailer.

Investigation showed the parallel board and connectors on the batteries to both be partially melted including the absence of several pins in the connectors on the board itself!

I later noticed (as you may have already) that the melted connectors on the board were the 6S connectors??? So somehow I had gotten the two 5S XH balance leads at least partially seated in the 6S connectors.  And I had done so consistently!!

I’m guessing that I managed to connect the ground part of the balance lead to the first positive wire on one or both, essentially grounding cell 1’s positive wire!  In any case whatever I did caused a enough current to flow through those pins so as to melt the plastic around them and de-solder some of them from the parallel board!

So main lessons learned:

  1.  Always wear your glasses when making these connections!
  2.  Don’t get in a rush.  There’s a lot of energy involved in this process and releasing it in the wrong way is dangerous!  Rushing anything involving RC airplanes is typically a bad idea.  If you don’t have time to take your time… don’t fly!
  3. Don’t count on the locator pins on the balance plugs to protect you.  Use your brain and your eyes to insure proper alignment!

While I was at the field I decided to cut the balance plugs (now mangled beyond use anyway) from the batteries as there were exposed pins etc… and I didn’t want to transport the batteries with any chance that a short might occur and cause another event in my vehicle or trailer!  I cut them off cleanly with minimal wire left exposed, one at a time, and staggered nicely so they couldn’t easily touch.  Also I was there for 3 or 4 hours after this occurred and the batteries weren’t swelling, getting hot or showing any other signs of distress so it seemed they might be salvageable and I wanted to examine them later on my bench.

 The next day at home I started going through and measuring the voltage and labeling each wire to identify the individual cells.  All measured in the vicinity of a storage charge level and by measuring each relative to ground I was able to figure out and mark the cell order.  Here’s my test setup with a battery in the midst of the labeling process.  I have the negative test lead clamped into the ground on the main load connection and that connection rubber banded down to keep it safely away from all the positive wires.

I found a place to purchase 5S extension leads, so as soon as I get those I will attempt to safely put a balance plug back on the battery.  Once I do that I can further test and cycle to insure the batteries are still good.  I’ll post again or add to this post when I finish that process to tell you the results.

In the meantime I’m wondering if a “safer” balance board would be a worthwhile investment?  Some have not only a fuse for the main connector (which mine does also) but protective self-reset able “polyfuses” on the balance connectors.  Right now those sound like a wise investment and I encourage you to consider that option if you start parallel charging.

Don’t get me wrong.  I don’t think that parallel charging is unsafe… just that it requires a bit of caution and attention to keep it safe!

Spektrum connect issues… resolved?

One of my largest aircraft currently is my Extreme Flight 74″ 12S powered Laser.  It is also one of my favorites due to ease of assembly at the field, unlimited vertical performance and the fact that it is capable of such beautiful aerobatics!  Sometimes it even looks good when “I” fly it!  Yep, the plane is certainly more capable than her pilot.

Really the only issue I have had with this plane for quite some time is on that occasion when I get it assembled and ready to fly… except the iX12 radio and 12 channel power safe receiver will not connect on power up!  It’s very frustrating.  It’s not that it has lost bind…  I’ve occasionally gotten it to work again by cycling power once or twice or even just taking it back home and trying again…  It’s was never obvious what I actually did to fix it… and sometimes it seemed nothing would.  It happens very rarely and usually if I just go through a rebind process it works perfectly from that point on for a long time.  This typically only occurs if the plane has been sitting idle for a period of times… week or months (like first flight of the spring) is the most likely time to have this occur.

So being as it is just getting to be good weather for flying on any kind of consistent basis here in Indiana, I just ran into this issue again!  This time I was at home and had decided to tinker a bit with the Telemetry when it once again refused to talk!  Power up the radio, power up the plane, pull the pin switches for both receiver and speed controller and… nothing.  Everything is sitting at centers and the usual sing/buzz from the servos but no link…  

I tried a couple of power cycles and still no luck so this time I decided to post on the Spektrum group on Facebook.  After several posts back and forth and a number of excellent suggestions, one gentleman pointed out that the power safe receivers would not link to radio if the proper number of remotes (he even said if just the A receiver was down, that would do it)  didn’t come on line and suggested checking the contacts and coating them with electrical grease to shield them from problems.  An intriguing idea so I went back to the airplane and did some more testing.  As I did so, I also noticed that I had not done my normal strain relief on these cables so I decide to take care of that before all was said and done.

What I found was that in fact the A receiver was certainly not linking up (no lights if I recall correctly… or at least no steady light) and once I re-seated the cable, everything linked up instantly.  Repeated testing showed it all working perfectly from that point on.

I have a fair amount of pride that few of my planes crash due to “avoidable” assembly and maintenance issues so I like to track these issues down and resolve them whenever possible and then apply the fix wherever it makes sense on the rest of the fleet.  This airplane for instance has redundant flight packs separate from the power packs that run the motor, nylon insert nuts on all of the ball linkage bolts, Telemetry monitored battery levels, etc… in order to make sure it is as reliable and survivable as is possible/reasonable.  So I decide to see if I could eliminate this issue for good.

After collecting the necessary items (all shown here except the liquid tape) I started to work to resolve this issue.

The process went something like this…  First pull the remote receiver (they are all attached with sticky back Velcro, so this is not hard to do) and the cable from the airplane.  Inside the box (I’m working in the living room so protecting the furniture/carpet from harsh chemicals and spills) I spray some contact cleaner into the end of each cable connector and into the remote receiver connector.  Once dry, I took a toothpick and forced some dialectric grease down into the holes on the cable connectors and then coated the pins in the connector as well.   I did the same on the receiver while still installed in the airplane… luckily it’s somewhat roomy in there… and then reconnect everything and wipe away any excess that squeezes out.

That should eliminate the possibility of corrosion in the future so once all was back in place I moved onto painting on some red “liquid tape” right on the back of the connectors and onto the first 1/4″ or so of wire for each of the four cables that connect to the remote receivers.  This helps to share the stress on those wires and eliminate the most likely break point for the connections.  The liquid tape will flex but doesn’t allow for kinking or pulling on the individual wires.  I have had a few of these wires break before but never had an issue once I applied this little “hack”.  I apply this while everything is plugged in typically.  If a bit gets on the receiver or over the outside of the connectors it doesn’t hurt a thing and simultaneously it can’t get in the way of the actual electrical connections if applied this way.

Here are the two plugs on one side of the receiver.

And here is one of my receivers sitting on top of the motor box under the cowl.  You can see how I have coated the connection, further protecting the wires against stress and contaminates to some extent.

We will have to wait and see how this works out.  I have high expectations that this problem is likely resolved and I feel very positive that this improves the likelihood that this plane will fly for years to come… or at least until I make a mistake behind the sticks!

UMX P-47 Electrical Issues Resolved

I received this UMX P-47 as a Christmas gift a couple years ago.  I have a warm place in my heart for the P-47 as my Grandfather helped put thousands in the air while working in the Republic plant in Evansville, Indiana.  I checked the markings and this model is based on an Evansville bird!  Excellent.

Here is what the little UMX looks like:

The P-47 was one of the primary work horses of WWII.  It was a favorite with a lot of pilots as it offered that most favored of qualities, survivability.  With plenty of armor protecting the pilot, a reliable air cooled engine and (as long as you had altitude) a dive speed that almost no other plane could match providing an escape if worse came to worse, a lot of pilots survived missions in a P-47 that would have had different results in other birds.   This led to a popular saying during WWII â€śIf you want to get the girl fly a P-51, if you want to go home to your girl strap on a P-47.”

It was also heavily armed with 8 fifty caliber machine guns and could carry 3400 rounds of ammo along with an impressive load of bombs equal to more than a third of what the B-17 bomber could carry and so became a favorite with the ground troops as well, providing a lot of support to the boys below.

For all these reasons, I love a P-47 and though I don’t get to fly it often I do enjoy it.  It flies well for its size, is fast enough to look like its doing what it should be, and it tracks nicely, I’m sure partly due to the on board AS3X stabilization.  It requires a good size space to fly indoors and can’t take too much wind so outdoors is limited, thus the limited flying time.

Starting last year I’ve had the opportunity to fly at one indoor venue over the winter months that is large enough to enjoy flying this bird in.  It was during one of these events that I started having a weird issue with the aircraft.

Occasionally, the bird would suddenly and completely lose power while taxiing.   This happened once and I thought I just had a bad battery.  The second time it started working again when I picked it up and re-plugged the same battery…  odd.    After that flight it went back in it’s portable hangar and sat for a couple weeks ’till the next indoor at which time I took it out and tried to fly again… It was only when the spark happened as I plugged in the battery that I recalled the previous issues.  I quickly disconnected a rather warm battery…  YIKES!  A close examination of the area helped locate the issue…

As you can see, the insulation has pulled back and several strands of the multi-stranded wire are trying to make some “non-approved” connections!  

To cure this problem I first cut off the remaining strands and then reattached them with the use of my handy “helping hands” soldering clamp.

 

Once that was accomplished I used some liquid tape to insure that no more unapproved connections were going to occur.

Then to help further protect the connection I applied some shrink wrap.  Here’s the final product.

I’ve since gotten 4 flights on the “Jug” without issue.  Unfortunately, with the recent outbreak of Covid-19… further flights are probably months away, but I am happy to report that the P-47 is back to mission ready status.  Here’s hoping we can all be healthy and back to this wonderful hobby soon.

Hangar 9 Carbon Cub 15cc ARF … Part 2

One of the first things I’m always concerned about with an RC airplane is just how easy it is to get flying once I get to the field.  I really don’t want to be fiddling with 15 bolts and nuts that require special tools to attach, nor do I want to have to crawl around on the ground to assemble the airplane, etc…  At least not if I have a choice.

With the H9 Carbon Cub I felt like it was going to just be to “fiddly” to assemble as designed from H9.  The wing attachment method with screws that would have to be put in from the bottom of the wing, up in a hole and then adding in the wing strut bolt attachments, the battery placement and mounting method which was going to have to be done reaching under the wing and into the cockpit area and then a screw inserted to hold it in place??  Did they really think I was going to do that for every flight?  I found it frustrating to do with no windows in place and the cowl off!  I certainly didn’t want to try this reaching in only through the door on the side of the cockpit.

All of this screamed out for some modifications so here is what I went with.  First, I decided that I wanted to reverse the wing mount tabs.  IE. I decided to permanently mount them in the wing and make the body end be the area where any attachment task was done.  To accomplish this I needed to remove the tabs from the body.  This was fairly quick and easy with the proper application of a ball peen hammer.  Here is one still mounted in the fuselage.

They have a shoulder on the inside of the fuselage so you need to push them into the plane body if you want to remove them.   A few raps and they pushed into the body and were easily removed.

A tiny bit of wood came off with them but not enough to cause any concern.  I then used the phenolic tab material as a pattern to make replacement pieces out of similar thickness aluminum.  Since I want them to extend a bit further into the fuselage so I can attach them on that end, each of mine are about 1/2″ longer than the originals and don’t have a tab.  I did drill the hole so I could attach them to the wing (I just intend to only do this once)!

Once all cut out and the hole drilled in each I did some sanding to round the corner and cut some slots into them so I would have a way to pull them together to keep the wings from sliding on the wing tube and opening up a gap between the wing root and the fuselage. 

Even with this mod, I didn’t want to have to reach up into the cockpit through the door and put screws in, rubber bands on or attach a tie wrap or whatever.  Between this and the need to swap out batteries I decided I wanted to have a removable top window.

This meant I needed to build some sort of frame to mount the window in and create a hatch assembly.  This sounds easy until you realize that the top of the cub is a curved surface AND the opening narrows as it goes toward the rear of the airplane!  So first step was to make some custom shaped window frames for each side.  I began by tracing the shape onto some light card stock (sometimes having a greeting card crafter across the shop comes in handy!).  I then proceeded to attach the template to some wood and then cut and sand to shape.

I then used some of my finer TLAR engineering skills (That Looks About Right) to make a rounded cutout in the bottom of these pieces in order to provide clearance around the wing tube.  After that I cut a couple of appropriate length 1/4″ square sticks to use as the front and back.  Each of these is custom of course due the aforementioned narrowing of the opening.

Once that was all completed and some careful fitting done, the frame was assembled (I laid all the pieces in the place in the top of the fuse and used CA to tack glue them together then removed them from the airplane and finished the gluing process). 

After a test fit of the full (one piece) window, I carefully marked and cut off the material for the top window.  Before attaching it, I colored the frame with a black permanent marker and then glued and clamped the window material to the frame with canopy glue.

This was allowed to dry for a few hours and then the clamps came off and I added a bit more glue around the inside edges to make sure it was not coming off anytime soon.  From there I started working on ways to mount the frame to the top of the airplane.  First I made a tab out of a couple pieces of popsicle stick and glued it to the front bottom edge of the frame at an angle so it would catch the front of the fuselage.  This prevents the front from lifting.  You can see this here.

I had to just do a bit of adding a layer of popsicle stick and then sanding a bit off to make it have a close enough fit.  More black marker to cover up the wood grain took care of hiding it.

The final stage involved another stick of wood on the back edge of the frame to add some “meat” to the frame (my original 1/4″ frame I felt was just to small) and allow for the attachment of a “handle/antenna” for easy removal of the top hatch when needed, along with a block of wood to house a magnet to hold down the trailing edge.  Adding some black pin striping around the edges to give it a truly finished look was the final step in building the top window/hatch.

After all this was said and done I decided with this easy access I could use a turnbuckle to hold the wing panels together.  Its very quick and easy to put in place and because of some fitting issues at the wing root of the port wing, I needed something to put a fair amount of pressure on to hold the wings where they belong.

Here are a couple shots showing the final product.  I feel like it came out pretty decent and I wouldn’t have been happy with the original setup.

Next time, I will discuss the bottom air vent I decide to add and a couple of other minor adaptations I made.

 

Hangar 9 Carbon Cub 15cc ARF … Part 1 of ???

A couple months ago my flying buddy Gary picked up a Hangar 9 Carbon Cub 15cc ARF that someone else had begun assembly on.  After he had done a bit more work on it he decided it wasn’t for him so I acquired it in turn.  I have always thought it was a beautiful airplane and wanted one so while I’m not sure how good a flying craft it will be, I decided to give it a go.

First, I had to decide what I would power it with.  For me that was an easy decision.  I doubt I will ever have another glow engine… expensive to run and messy.  Other than having good memories that pop up when I smell hot glow fuel, there’s just no good reason I can think of to put one on an airplane these days.  I may do another gas powered RC airplane one day, but not glow.  It doesn’t hurt that I happen to have a slightly used Power 60 and 100A Castle ICE sitting in a drawer.  Decision made, I started going through the manual and deciding what still needed doing to get it flying.

In addition I needed to go over the airplane and see what the previous owners had done that might need some attention.  I also started researching the airplane online and noting what I might want to add or modify.  So far I’m still not quite to full flight status!  Like most of my builds, this one has been interrupted, delayed waiting on some parts or just to give me time to decide how I wanted to do things, and has taken about 10 times as long as the manual suggests!   I’ll start to add some articles soon detailing the changes/issues and challenges I’ve had getting the Cub ready to fly.

 

Mini Convergence VTOL – First forward flight, and first repair!

Back around Xmas a relative gifted me with a nice little micro flyer for indoor use.  It was definitely a beautiful little plane… as a matter of fact it was something that I liked so much that I had purchased one for myself just weeks earlier!  So back to local shop I went to make a trade… and on a whim I picked up a Mini Convergence VTOL from E-Flite.

I flew it a couple times over the winter at some of our indoor events but I was not about to try forward flight in the limited space available so it sat mostly unused through the winter and for most of the summer before I really recalled it was over there in the corner in a pile with my other indoor flyers!  After I dug it out and charged some batteries I took it out to the field, rechecked all my programming to find the right switch setting to get into a forward flight mode and lifted off.

Forward flight mode went well and I was getting a pretty good handle on how the plane handled life as a fixed wing when the radio timer started warning me I should start to think about landing.  I slowed a bit and then flipped the switch to go back to vertical flight mode when things started to get “interesting”.

The plane began to immediately flip end over end and no control input made a lot of difference.  It didn’t fall very fast but all I could do was throttle down when the ground came up to grab the airplane.

Back on the bench here is a view of the culprit…

As you may have noticed there’s something missing on the rear motor… two things in fact.  The prop and the spinner nut!  No wonder if flipped end over end!  There were also a couple of foam “piercings”.  One in the wing and one in the canopy.  Neither of those are any real concern.

Luckily the bird comes with two spare props.  The rear prop, I found, is the same as the port/left prop.  This has it’s pitch in what I would consider the “standard” direction for aircraft with a counterclockwise rotation creating rearward/downward thrust.  Luckily, I just happened to have an aluminum prop nut/cone with the correct thread in the shop and the plane comes with one of each type of spare prop so that problem was quickly solved.

Unfortunately when I powered the plane back up I quickly found another issue.  The port side motor did not rotate up into the same position as the starboard. 

I quickly realized something was not right with the servo that performed the “tilt” on that motor.  Opening it up, you can see why.

To get this view I had to remove that servo which required removing a couple screws to get the servo unmounted and a few more to remove the plastic faring that covers the bottom of the boom.  Also, I disconnected the linkage and finally I had to split the tape with a razor blade (careful not to cut wires) and once removed, open up the servo.  Some of that disassembly is shown below.

Reassembly had to wait a couple weeks but was not particularly challenging.  For once I didn’t lose any screws, linkage, etc.  The only real gotcha was to make sure you have taken note of where and what orientation the plug goes into the receiver/main board and be sure to power up the aircraft and allow it to pivot the servo to the starting point so you can line up the servo arm on the new servo so that the two engines are pointed in the same direction for startup.

So, moral of the story.  When you read on line that folks have had some issues with the prop nuts loosening up and you should check them before each flight… listen.  For my part, I decided to do something to help the nuts stay in place so I put a bit of clear finger nail polish on the threads of all three of the motors before replacing and tightening them down.  I find it works pretty well as a thread locker for such things without risking any damage to plastic (like the props).  Some thread lock compounds have been known to make plastic brittle over time!  It is also fairly easy to muscle the nuts back off with the finger nail polish but in my experience does a fair job of eliminating any loosening due to vibration and the like.  IE it can broken free again but won’t generally fail under normal use.

I’ve made one flight since this repair and the aircraft did well.  So if you have one of these, do yourself a favor.  Go unscrew all three prop nuts and find some non-permanent thread lock (or raid the wife’s nail polish stash) and take out a little insurance.