FMS T-28 Trojan V4 Yellow 1400mm – Cursed?

A club member recently picked up the FMS 1400mm T28 as a step toward getting back in the air.  He’d been ill and hadn’t flown much for most of a year but he has flown a bit of everything and now does mostly Turbines so he wanted a war bird with retracts and flaps… something to get his fingers re-awakened but still with the extra “complications” of flaps and retracts so he wouldn’t get out of the habit of using those!  After a bit of debate he went for this bird:

I never did hear the whole story but apparently, right out of the box the plane had issues.  I heard stories of at least one speed controller swap, retract issues and a bad aileron servo…  I don’t know exactly the list or the sequence of events but he quickly ran out of patience to troubleshoot all the issues and offered to sell the bird at a bargain basement price. 

A second club member (let’s call him Gary) picked it up and got a warranty swap on the bad aileron servo which he replaced.  He planned to bring the plane to my shop to troubleshoot any other issues he found but as fate would have it, he was in the midst of one of his infamous multi-part swap/purchases and the plane one again changed hands, landing now with Steve.  One part of the plan didn’t change and that was to get it to my shop for a thorough once over.

Once the plane arrived Steve and I started testing and going over the plane to see what all was or wasn’t working.  We did a quick bind and testing of the plane and quickly found one issue… NONE of the three retractable retracts actually did anything!  Not a buzz, beep, wiggle or shake to be seen!  No amount of coaxing, servo reversing, battery swap, rebinding, driving with a servo tester or anything else would make them budge. 

Over the course of a few days I traced down all the wiring to each retract and nothing would convince any of them to move!  This is not as simple as it sounds as the receiver drives a distribution board in the body of the plane which then is wired via a multi-wire connector (looks like a balance connector on a 5S lipo) to another distribution circuit board/box buried in the wing root where the retracts, flaps, ailerons and lights for each wing are plugged in.  This is all starts to quickly look like a spaghetti bowl but eventually I pretty much had it mapped out in my mind.

Eventually I plugged in a servo at the wing root connection and proved that signals were getting to that point as the servo moved appropriately.  I did this for all three retracts and every one of them tested the same… bad retracts!  Now I have no idea how the retracts got to this point.  I’m fairly sure they are not shipped in the down position and all were now in that position.  They did not stink or have obvious damage so it was not obvious if they were somehow abused but it seems crazy that all 3 would fail in this manner.  I guess we will never know.

Fast forward a week or so and 2 of the 3 needed retracts have arrived at the shop.  Swapping them out is not overly difficult.  I found the simplest way was actually to completely open up the retract housing (split it after removing the 4 plate screws AND the 6 small diameter screws that hold the two sides together and just replace the whole trunion, strut and wheel assembly. 

Seemed easier than fiddling with all the set screws etc… especially for the nose gear with its’ C clip.  As best I can tell the electrical parts are all the same for nose and mains so I swapped out the Port main and then the nose gear and both worked perfectly after that!  So, confirmation that they were indeed bad.

Two or three weeks later another couple retracts came in and I once again dug into the T28.  Third retract install complete and it is working… Reassemble everything and then suddenly it doesn’t!!    Double check all connections and no go… time to take the plane apart again and recheck all those connections.  Re-seat all the connections and everything works fine again. 

OK, so back together and checking everything and what’s this… both Ailerons move in the same direction??  Long story short (this story is long enough) the servo that was supplied as a warranty replacement turns out to be a reversed servo!  So call the local hobby store and order a replacement (correct) servo… wait and then take it apart again and swap that servo out.  Now it should all be good, right?

Reassemble, checking at each step, and all looks good with the new servo functioning correctly until after the final wing assembly.  Plug the battery back in to do a final check and what the what??  When the battery is plugged in nothing happens… and I mean nothing!  No lights, no beeps, nothing!!  Try different batteries… nothing.  This is an ARF… when will we get to the ALMOST part of this??

At this point my cursing skills are well exercised and I’m beginning to think I might go pro…  Something with the new servo??  One more time to check all the wiring… disassemble the whole plane again and trace wires when I notice something.  One of the “wing root” connection boards looks like this:

Bare wires seem bad… especially when some of those little hair thin wires look like they might be touching?!  I have no idea but my theory now is this is what started all the issues… It’s possible that these wires were pulled out as repairs were done… by me, perhaps… by the other 2 guys that have had their hands in the plane… maybe.  But to my eye the insulation on the wires seem to have none of the white “goo” on them and a couple of the stray wires do.  I think this was something the factory missed on.  I’ll never be sure.

So while I have the plane plugged together BUT still all connected, I unplug the white XH style connector that feeds this side of the wing and try again and…  Beeps, buzzes and all the other “correct” noises issue forth!!  I think I may have heard some angels singing… just sayin…

So under a magnifying glass I went through and separated all the wires and painted that connection point with liquid masking tape.  Once finished the final product looked passable:

Once reassembled it all looked great.  Flaps, ailerons, rudder, throttle… check.  Retracts… all three down and locked and back up again… check.  This thing might just fly yet!  Just as I was doing the happy dance… Hey, why is that landing light not on…  At that point I had to make a decision… smash this thing into a hundred pieces and make up a good story for Steve on what unfortunate event had claimed the ill fated T28 or one more time time through the wiring.  OK, so this one was simpler.  About a 90% chance that the 2 wire, unkeyed connector (OK, its color coded but why not use a standard servo connector so idiots like me have a better chance to get it right?)  is plugged in backward.  Yep, that did it.

After all that, she looks to be ready to fly… finally.  After purchasing the plane at less than half of what it originally cost, Steve has spent enough on retracts and a servo that he is pretty much up to having paid full retail and then a bit!  If I charged minimum wage, I think he’d have to tell the wife “Sorry honey, no Christmas this year”!  Good thing we do this for fun.

Hopefully all this will be worth it when this bird take to the air.  T28s are typically great flyers so we are looking forward to seeing it in the air.  Maybe we should schedule an exorcism instead of a christening!

Gary’s Hangar Nine Corsair with Evolution 777

Recently visited one of the “Garys'” to make a stab at getting his Evolution 777 4 stroke, radial, 7 cylinder motor to run at other than 20-35% throttle settings.  Previously that was the “best” we could get.

But today, here is what we got to…

 

https://youtu.be/G79xyCGJb-M

 

This is a much superior result.  So what was holding it back?  On the previous runs we had been running some older fuel and also been advised that we needed to open up the high speed needle a bit… but undoubtedly the key factor had to be the replacement of all 7 glow plugs!

A bit of overthinking (perhaps) had led someone to decide that the brand new plugs in the motor needed replaced before the first test run.  And someone else advised that the OS #8 was the best plug for ALL glow motors!  Perhaps that statement might have been a bit… overstated!?

While I agree that the OS#8 has long been one of the best all around plugs for a large majority of smaller displacement 2 stroke glow motors, there are also reasons that manufacturers recommend hotter plugs, colder plugs and very pertinent here… specialized 4 stroke plugs for some motors.  So by moving back to the provided 4 stroke plugs, fresh mixed fuel and some judicious tweaking of the needles per instructions from the support folks at Horizon Hobby… and we are now officially into the break-in process!

This Corsair might actually get off the ground… eventually!

Motion RC P-38 first flights… and the resulting damage!

A few days ago, the two P-38s finally got to go visit the field.  The last couple adjustments that were needed seemed to be finished up and there was nothing left but to fly them!  Several club members gathered to watch the inaugural flights.

My green P-38 with the addition of invasion striped on the wings was first to go.  I had 2x3300mah batteries on board pushed all the way back as a best guess center of gravity.  The final run up up of each individual motor/speed controller was accomplished in the pit area just before taxi out for take off.  I must say the wire connections to each wing are somewhat tedious.  There is not much extra wire to make connections and my hands are not very small.  Also the lighting connectors are NOT polarized plugs so you also have to be very cautious of plugging those in with the proper polarity.    Then the tedious stuffing of the wires into the small opening (individually… there isn’t room to do them all at once) while simultaneously sliding the wing panel onto the body.  As I said, tedious.  Of course you have to do this upside down and I was trying to be very careful not to put any pressure on the canopy (removed that) or the props (suspended off the edge of the table).

 

Finally, all assembled and I immediately noticed that it was a bit difficult to turn left on the ground… I suspect the cross wind from the right hitting those two big verticals is responsible for that!  But she lifted off pretty quickly.  I had to do quite a bit of aileron trim to keep it level and some elevator trim to keep the nose up.  I’m betting the aileron trim is a result of the inboard wing edge that is warped downward on the one side.  Finally, all level and flying smoothly I started to pull a loop but decide not to since it appeared that my elevator travel was a bit low and there was not a blazing amount of spare power either.  No big deal, I’d been flying for a few minutes so I might have been getting some sag from the batteries by then, so I just decided to get back on the ground.  First pass I came in without flaps and it was sinking awfully quick while still flying pretty fast so I went around and dropped half flaps and tried again.  My guess for elevator mix must have been about right and I came in a bit slower but still with a pretty fast sink rate…  That made for a moderate “hop” and then too much speed as I ran off our Geotex into the grass at a good clip.  That arrested the speed within another 15 feet or so but as it did so, one of the mains folded up!!  That was very disappointing as I really thought it wasn’t a terrible landing for the first attempt.

Here’s the retract with a bit of foam still attached… but not much.

And here’s the foam socket with (apparently) very little glue.

Further inspection showed that the gear mount had separated from the foam from (in my opinion) a notable lack of glue…  There didn’t seem to be any other damage but I was obviously done for the day.  I try to minimize repairs at the field, generally opting for moving on to another plane if the program is just casual flying so I went back to help Kelly work on his P-38.  Another impression I had after the flight was that the plane flew somewhat “heavy”… i.e. it flew like a warbird.  I was hoping for a bit more of a “foamy” feel to the plane but it was not totally unexpected with the modest wing area compared to the weight of this airplane.  I had read where some folks talked about it flying fairly light on the wing and coming in slow but that was NOT my experience.  Those guys must be hard core warbird flyers who are accustomed to the heavy wing loading of that type of plane.  For me, it seemed heavy but I don’t think I’d want to fly much less battery capacity as flights would get very short I would think.  Based on just this flight, I don’t think my 3300s will get me much more than 6 minutes, but I’ll have to fly a few more to be sure.  I wasn’t paying strict attention to that with all the other maiden flight checks and nerves going on.  Finally, the P-38 does not like to turn with just aileron.  It needs either some rudder mix or at least a pilot with a left thumb that doesn’t fall asleep from lack of use once airborne!  I fly a few other planes that like rudder in a turn (a Carbon-Z Cub, a Telemaster) so I adapted to that fairly quickly, though it will take a bit of flying to get just the right feel for it.

Moving on to Kelly’s P-38 in “Pacific Silver” we went through the same preparations and then he was off the deck.  In short order he was having problems getting the plane to turn and there were a couple times when it looked like he might not be able to control it to get it back down safely.  Finally, he was able to herd it onto the Geotex with a fairly fast but mild landing.  He too ran off into the grass and immediately one of his main retracts folded as well!  This aircraft definitely isn’t built for any but the smoothest runways!

Later inspection showed his retract to have a pitiful amount of glue as well, so apparently I didn’t just get the one built on a Friday!  Between the battle to keep the plane airborne… it seemed to be constantly yawing to one side… and the retract issue, Kelly was very disappointed with this aircraft.  He was running a single 5300mah battery and it certainly appeared that his airplane flew similarly to mine as far as landing speed and overall handling even with the somewhat lighter pack.

I am working to replace the retracts in both planes with a bit more generous portion of Foam-Tac and hoping we can keep those in place.  We are extending the Geotex runway soon at our club field so hopefully we won’t run off quite so easily anyway but it is disappointing that these are so fragile.

I have a theory on why Kelly’s plane seemed to have a serious yaw issue… more on that after some investigation.  So far, neither of us is particularly fond of the P-38s.  Hopefully we can work out the wrinkles and get in some more satisfying flights soon.

Graupner MZ-24 Radio — What???

My flying buddy Kelly, who I’m pretty sure considers me his personal “RC Aircraft Mechanic and Radio Setup Technician”… decided some time ago that he wanted to get a new radio system for his RC needs.  I know he has had good experiences with his Graupner charger and is a big fan of German engineering in general and so had high hopes when he ordered his new radio system.  He even talked to me first to insure that I was up for learning a new system and I said yes….

I have programmed many RC radio systems over the past 15 years or so. Airtronics RD6000, RD8000, Hitec Prism 7, Futaba 9CAP, Multiplex EVO 9, JR9303 and Spektrum DX8 and DX18 are all transmitters that I’ve spent time programming.  I’ve spent significant time and effort setting up multiple aircraft from trainers to multi-engines and delta wings to 3D aerobats on these radios and now I can add the Graupner MZ-24 to that list… or at least I’m trying!

Some random thoughts on my experience so far.

The MZ-24 is NOT a 24 channel radio.  For EVERY other radio in my list above you could probably correctly guess the number of channels by picking out the number in the radio name… but not the Graupner.  For some reason the number of channels you can control is 12… you can now decode that the MZ-18 is a 9 channel system, maybe?.  Kelly wasn’t fooled… he’s definitely a guy to research his purchases but I was fooled for a minute or two.

What Kelly thought was a German radio was apparently designed and built in South Korea?  Now that’s not a bad thing in my book… I’m pretty sure that more than half of the electronics in my home were designed and built there and I wouldn’t keep buying them if I didn’t think they were great products….but this radio…. maybe not my favorite effort from our friends in South Korea.

Setting up the flap system on this radio has been a multi-week odyssey which has ended in…. success… but only after completely abandoning the built in flap system functionality!  Apparently, setting up the flap system to do a simple 3 position flap setting with elevator mix is completely beyond my ability using this radio if I try to use the built in flap system.  Even after a few exchanges on the phone and via email with Graupner support I could not reliably make the flaps worked as I wished.  Setting the end points of the flap function is apparently impossible, and simple reversing of the function and strange things like changes in speed through the travel of the flaps are a couple of the  challenges I faced when trying to use the flap system.  Take my advice and just leave that function alone.  Just assign the channel, set the endpoints and sub-trim to establish the motion you want.  Slow the servo with the servo speed function and then build your own mix for elevator or whatever else you need.

Programming the telemetry system on this radio is… just odd.  While most other functions are configured in a somewhat intuitive method… when you get into the telemetry system you are confronted with screens of text that look like they are something from a 1970s computer application… i.e. from the days when computers didn’t yet have a mouse attached or a graphical interface.  Gone are all the pretty colors, graphs and symbols.  Absent are any understandable directions… at least for the simple voltage monitor we wanted to use.  Even the list of “alarms” are just labeled with numbers.  What each number represents is cataloged where?  Imagine how easy it could be to program a telemetry system if you a full touch screen color screen with audio prompts available…  Oh, that describes the Graupner radio!!  Unfortunately what we get is text only…  Did the graphical interface team all quit mid-project?

The range of receivers available, reasonable pricing as I recall and apparently solid build quality… even the various ports and options available… All would give the impression of a high quality, easy to use, good value, complete RC system.  To bad that it seems this product never got “finished”… or at least that is how it seems.

We are going to continue to work with this system and just see how it goes… at least until or unless we run into actual RF issues, which I don’t expect.  Here’s hoping Graupner does some more development and sorts out the oddities in the user interface.  The potential is certainly there.

For my part, I think I’ll stick with my Spektrum DX18.  I think both it and the DX9 are great radios that do about anything you’d want and who’s interface is far superior to the Graupner… even without a touch or color screen!

 

Freewing 80mm Super Scorpion EDF Jet

Recently, My flying buddy Martin has decided to branch out into some ducted fan electric craft and one of his first is the Freewing  80m Super Scorpion from Motion RC.  Martin had the new aircraft shipped to my shop and today he came by and we did most of the assembly.  

The first observation I would make is that we spent about 4 hours today doing assembly and we got to the point where all we need to do is plug in the receiver and set the throws and it will be ready to roll.  Maybe we could have cut it back a bit but don’t believe the place on the website that says assembly time is 30 minutes!  Just scroll on down where it says 3 hours and you are in the ballpark.  The other specs listed on the site seem to be accurate, even down to the ready to fly weight.  Measured with a 4500 6S on board, we measured Martin’s aircraft as just a couple of ounces over 5 lbs just as the web site reports.

Similar to the manual for the P-38s that I recently got from Motion RC, there is a lot of “stuff” in this document that describes assembly that is already done out of the box.  This is distracting and it sometimes makes it hard to figure out what the next “required” step is in the assembly process.  Unlike the P-38 this model however does not have a full assembly video on the web site and luckily it isn’t needed as there just aren’t that many pieces and assembly is not all that complicated.  Just walk through the manual and keep skipping forward when you read the parts that are unneeded and you’ll have little trouble.

There are only a couple of places where I can give you some advice that might not be obvious. 

  • When you put the screws in to attach the wings to the body, be careful to route the wires appropriately then be very careful that the screws are actually going into the holes in the plastic.  The best way to avoid this is to just start each before you fully tighten any.  A simple thing, but easily overlooked.
  • When you attach the vertical fin, insert the front screw first but only a couple turns.  Then do the side screw and tighten both down before installing the screw from the top.  Otherwise it is very difficult to get the top screw to hit the pre-drilled hole in the wood plate that it attaches to.

And a critique or two for the manufacturer and distributor.

  • Somehow there were only 2 of the 2:1 servo connectors and 1 3:1 servo connector included in the kit, even though the manual clearly indicates there should be 3 of the 2:1 connectors.
  • On the website it is implied that you can remove the wings and elevators and the vertical stabs (presumably) in order to carry it to/from the flying field.  “Removable wings and vertical stabilizers for convenient transport”.  Perhaps this could be done a few times in order to ship the aircraft from place to place, but these self tapping screws and plastic and wood into which they are screwed are not what I would expect if this were actually the case.  I would expect most folks are only going to take these screws back out if a repair is needed.  Anyone who needs to take this aircraft apart in order to get it to and from their flying field should look for a better alternative.

Since the high today in our area was 38 degrees (about 20 degrees below my minimum standard for comfortable flying) we don’t yet know how it flies but here are some pictures of how it looks.  Some highlights I would point out are the nice shock absorbing struts, the cockpit detail and the attractive and hopefully easy to see color scheme.  Though the aircraft is not quite as large as Martin had assumed, I think he is still fairly happy with the overall look and build quality of the aircraft.

Here is the nose gear showing the nice shock absorbing strut

 

Here’s a shot of the actual functioning inlet that feeds air to the ducted fan

  

And the finished product.

Looking forward to see how it flies.

 

Motion RC P-38 – outboard flap issue resolved

So, the silver P-38 sitting on my bench has one flap servo that appears to have the servo arm incorrectly installed.  See my previous post on this topic for details.  Motion RC P-38 – outboard flap issue

I was gathering the necessary tools to slice into the plane as described but decided to do a bit more research and found that others had pulled other servos out of the P-38 and reported that they were glued to the paint, not directly to the foam.  This gave me a bit more confidence that it would come out without tearing up the foam.

My first thought was that I would have glued the servo in directly to the foam…  which would have made this worse… so good thing no one asked me!  So with this new information I went back to the shop and made a careful incision all around the edges of the servo where any glue might be holding it and then with a pair of pliers I just grabbed on and started yanking and wiggling…

As advertised… the paint stuck to the glue and thus to the servo but the foam is largely undamaged.  With this I was easily able to then remove and replace the arm into the correct position and things then lined up nicely!!  Another hurdled cleared.  Glad I didn’t get in a rush about cutting into that wing!

We are now much closer to flight on these two birds and I’m starting to get back closer to the initial excitement to fly them that I had when we placed the order.  Just another session or two at the bench to get all the throws and rates set up and we should finally be in a flight worthy status… just in time to wait on the weather…

Motion RC P-38 – outboard flap issue

My buddy Kelly decided to put his P-38 on his new Graupner MZ-24 radio.  This gave me the opportunity to play with his new radio which posed some challenges but I’ll save that story for another time.  The issues with programming the MZ-24 were eventually resolved but then another issue with the P-38 was found.

The P-38 has a control board that acts as a 4 to 1 connection for the 4 flap servos.  This means that all movements (including centering and trim) affect all flap servos equally.  Unfortunately, one of the outboard servos is not set for neutral at the same point as the others.  Here is a picture of the two outboard flaps with the servo arm at neutral…

Notice the control rod in the picture above lines up with the edge of the servo case protrusion.  In the picture below, it is entirely inside the case protrusion.  I.E. the servo arm on one is much closer to perpendicular to the wing than on the other.

Because of this, the corresponding position of the control surface is impossible to match up between the four surfaces involved.  I can match up either endpoint on this one flap by adjusting the linkage but the further you move from that position, the more magnified the discrepancy between this surface and the other three becomes.  It’s simply geometry.

Typically, the solution to this is to simply remove the servo arm and rotate it to a matching position to the other 3…. assuming this difference is “one tooth” which I’m hopeful is the case.  In this installation the problem is compounded as the servo is sitting flat in the surface of the wing with the arm retaining screw pointing toward the wingtip.  I understand this orientation is likely a necessity as the wings are not exceedingly thick so orienting the servo this way makes sense but to every design decision there is a trade off and this one results in severely limiting access to that screw.  An additional compounding factor is that the servo is glued in place which makes accessing this screw nearly impossible without some more drastic measures.  I know this is common practice in foam models but it is NOT a practice a can say I’m fond of and this is a perfect example of why.

I tried to pull the servo out, but the glue appears to be underneath the servo and I don’t think I can remove it without risking tearing a hole clear through the wing…  So the only approach I can come up with is to cut a triangular groove into the bottom of the wing so that I can get a screwdriver in there and remove the screw so that I can rotate the arm to the proper position.  I’ve been looking at it for days and have come up with no better ideas so soon I will start the necessary surgery and hope for the best.  If I can make the cut precisely and neatly enough with a sufficiently sharp blade, I’m hopeful it can be replaced with minimal structural or even cosmetic damage.

I guess I need not point out that better quality control could have avoided this issue and perhaps Motion RC would do something to take care of this issue if I called but honestly what could they do?  Sending a new wing is the only option that would do us any good and with the decals already in place that makes a bit more work and I am hoping this will end up being an easy fix.  I hope the hardest part will be stealing myself to cut into my flying buddy’s brand new airplane!  I’ll post further post-op.  Wish me luck.

Motion RC Pacific Green P-38 progress – near flight worthy

After an email exchange with Motion about the sheared screw in the back plate of one of the spinners, they shipped me replacement spinners and screws.  While I still dislike this setup, I’m going to give it a try for at least a few flights.  To replace these with something more appropriate in a two blade, as discussed in an earlier post, is just more than I want to spend at this point on this airplane.

Moving forward with replacing the screw led to applying the wire covers on the bottom of the plane.  I deviated a bit here and just used some clear packing tape to hold these in place.  I’m not entirely sure how well that will hold up but we shall see.  I hesitate to glue those in case I need to get back in there and rerun any wires or the like.  This was followed by adding the antenna on the nose as well as the counterbalances on the elevator and the “decals”.

The decals seem to be a mixed bag on this bird.  First, the good news.  Many of the decals seem to be vinyl or something very similar and they seem to adhere well and look fairly good.  If you haven’t dealt with vinyl before, these are not peal and stick decals.  You do not float them off the backing like the plastic models of old.  Nor are they applied by just peeling them off the backing and rubbing them on.  You do that, but then you peel the top, clear plastic looking material back off the plane and leave the vinyl behind.  This can be a bit tricky at first.  My tip is to use something like a pencil eraser of the round screwdriver handle end to rub with a bit of force in order to get the vinyl adhered to the airplane and then be careful how you peal the carrier off.  Watch for the vinyl to lift back off.  If it starts to do that you need to rub some more!

The vinyl parts are the majority but there are some of each of the others as well.  This is very odd.  The decals for the props seem to be the old water float decals and in my opinion they are the worst of the group.  The props are not perfectly smooth with a fine grained surface and this makes it that much harder to get a good adherence with these water slide type decals.  These are the worst of the group and I really don’t understand this choice as these are the most likely to fall off I would think.

Finally the stars and bars seem to be just a peel and stick type.  I would much have preferred vinyl for these as well but they look decent.  I just question their longevity.

There is a full page diagram included that shows where to put all the small vinyl decals and the opposite side shows the relevant parts of the aircraft from various angles in order to allow for positioning of the nose art, kill marks etc…  It has been noted that there are some minor errors with the placement of the small decals for things like hatch cover markings, no step and similar items.  I don’t plan on applying all of them as most are invisible at more than 3 paces anyway.  If we get a lot of snow and I’m stuck at home for a full day in the next month or so I may go back and apply a few more but in my opinion they don’t add much.  I did the nose art and fuel cap markings, kill marks and few other larger markings and stopped at that.  The rest seem to be diminishing returns in my book.

I also had the displeasure of applying the slide on decals to the props.  I hate that these hardly seem to stick at all and appear to be the lowest quality of the markings as they are also some of the most visible when the plane is sitting idle and add a nice look to the props.  Unfortunately one of mine has already fallen off and I’ll be surprised if they last past flight 3.  Oh well, as we say at the field: “50 feet and 50 miles an hour”  If you can’t see it in that condition it isn’t worth worrying about!

After a batch of other sundry tiding up, labeling the wires etc… I’m pretty close to flight worthy.  Here’s what she looks like sitting in the new “up stairs” shop.

She’s looking pretty good.  Still not sure what to do about adding some invasion stripes on the wing and booms… I think it will need it for better visibility but I hope to get a few flights in before I get involved in that.  I’ve never been much of a painter so not looking forward to applying those but it may become a necessity.  Unfortunately there are no decals or vinyl for those included with the plane.

I think about all that is necessary before the first flight is possible is to set and double check the throws on the primary flight surfaces and check the speed controllers are calibrated/coordinated.  Beyond that there might be a few tweaks toward getting the telemetry set up the way I would prefer and checking balance with various battery options and it will be as ready as I know how to make it.  With a pair of 3300mah batteries on board it weighs in at 8lb 6ozs…  I’m expecting very war bird like performance but hoping (maybe wishing) for a bit lighter feel than my 24lb Mustang!  ðŸ™‚

I’m taking a break from this one for a bit and working on getting the Pacific Silver version ready for Kelly.  We are having some issues getting his Graupner radio to do what we need and I keep missing out on making contact with Graupner support to iron it out so it has (pardon the unintended pun) stalled out for the moment.

 

 

Motion RC Flightline P-38 – Hinge fix

After some communication with the tech support folks at Flightline, I embarked on a plan to repair the poorly glued aileron hinges.  To better explain the issue, here is a short video showing the undesirable motion of the aileron on Kelly’s silver P-38:

The Motion RC folks explained that the hinge in these planes is basically a rod that runs through the aileron with tabs that pivot around that rod extending into and glued (ideally) into the wing.  It’s these tabs that are apparently not secured very well in the two P-38s we received.  They suggested that I carefully drip some glue down into the pockets in the wing.  The following is how I carried that suggestion out:

This was unfortunately not unique.  At least half of the aileron hinges across both aircraft were found to be loose to varying degrees.  This is disappointingly poor quality assembly by Flightline.  Of course, the fix was not terribly onerous but I wonder how many folks have assembled the airplane and only found out this was an issue when the airplane shed an aileron or worse??

In any case, if you build or have built and are flying one of these I highly recommend you check your aileron hinges before you fly.  This could easily cause a loss of control with serious ramifications.

Motion RC / Flightline P-38 assembly… more issues crop up!

As my buddy Kelly and I worked yesterday on the latter stages of assembly, we came upon yet another issue with these birds.  As he was assembling the linkages and connecting them up, he noticed that there was some slop in the movement of the ailerons.  Here is what we found:

Above is the Aileron with the aileron centered and the servo holding the center position.  I am applying very light pressure to maintain this position.

Here I am applying a small amount of opposite pressure.  Again the servo is holding center position and the linkage has almost zero slop.  All of this motion comes from the hinges sliding around in the pockets (I think inside the aileron versus the wing…)

In this case, both of the hinge points (I think that is what they are) on the inboard end of this wing panel seem to be completely unattached on the aileron end.  I am rapidly becoming very disappointed with the quality issues on this airplane.  This is my first FlightLine and Motion RC purchase and I’m not exactly encouraged to spend more money with them at this point.  Still, I have had some issues with other manufacturers aircraft “out of the box”… and some of those have become my favorite planes.  Often this is based on a combination of flight performance and support from the manufacturer so I will withhold any final judgement until I get some response from Motion RC and I have a few flights on the bird under my belt.

Hoping for better things…